Description of my Ball Screw Conversion
I decided to try saving some money and make up my own ball screws from
material I purchased from McMaster Carr. I will add the drawings and dimensions
to this page as I have the opportunity. My first plan was to try grinding
the screw stock to the required dimensions using a 4" 90 deg grinder clamped
in the vice of the ShopTask. After messing around with this proceedure
for a few weeks I cam to the conculusion that it was too slow and that
I was not able to get everything set up rigidly enough to get the finish
I wanted.
So, it was off to plan B. I figured if I heated the end of the screw to a nice cherry red and let it cool nice and slow the ends of the screws would be annealed and I could turn them with a carbide bit. Well, guess what. the screws are air hardening steel and I managed to achive was to increase the hardness od about 6" of my screw stock!
Well, plan C. I decided to machine the ends out of some round steel stock and then to attach these machined ends to the screw stock with a coupler sleeve and have a friend TIG weld them in place. I proceeded to turn out the ends and make up some coupler sleeves. On the Y axis I sized the coupler to be a press fit to the machined ends and I used an arbor press to put them together. I made the fit to the screw stock a shrink fit and heated up the coupler and slid it onto the screw with a little help from a hammer. If I was doing this again, I would use larger diameter (aprox 3/4") steel rod and make the couplers and intregal part of the extensions so there are only 2 welds per screw instead of 4. The disadvantage is you have to turn more off the rods, but the extra machining time would be worth the effort. On the X axis I made the coupler to be a loose hand fit onto the screw stock and this proved to be the better method. On the Y axis I had to get the runout on the extensions down to a reasonable number before I had the shafts welded and of course they moved so I had to realign then again after everything else was complete. To weld the X axis we had to come up with a way to fixture the parts during welding as the coupler fit was too loose for the extensions to hold position by themselves. So, we ended up putting the screw in the lathe 3 jaw chuck and using a dead center to align and hold the extension. This method worked far better, requiring me to only align the shafts once and the amount they were off was less than the I got on the Y axis that was press fitted. I ended up with < .005 runout on all the shaft extensions.
Now for a further update after about 4 months of use.
From the day I installed the ballscrews I would get a cracking type
noise on the X axis much like the sound you get when adjustable cup and
cone ball bearings are adjusted too tight. I attributed this to a ball
nut and screw combination on the X axis that was on the tighter side of
the tolerances as the X nut did not move as smoothly with the shaft off
the machine as the Y axis nut did. Over time this cracking got more frequent
and even seemed to cause some binding and lost steps on the X axis. So,
I finally decided to pull the X axis lead screw and see if I could figure
it out. With the lead screw removed the ball nut now moved smoother than
ever and I noticed nicely polished tracks where the ball bearings ride
on the screw stock in place of the original black slightly textured surface
finish. Looking at the adapter I had made to connect the ball nut to the
table I noticed that the threads the ball nut screws into were cut at a
slight angle causing the ball nut to be cocked at an angle to the screw.
I made a new adapter and this time I made sure the threads were straight
by holding the adapter in the 3 jaw chuck and using a center in the tail
stock to make sure the tang end of the tap was in line. I reassembled everything
with this new adapter and while putting it back together replaced the small
allen set screws in the saddle clamp and the CNC belt drive gear with good
quality USA screws in place of the soft screws originally on the machine.
I also drilled and tapped the CNC belt drive gear for a 2nd set screw to
try and keep the gear from getting loose on the X axis shaft. I am happy
to report that the X axis is now smooth as silk and has no binds and no
more cracking noises.
Bill of Materials
ball screws - part# 5966K26 2- required
ball nuts - part# 5966K16 2- 2' lengths required for plan C
You can find these on the McMaster Carr web site by searching for the
term "ball screw" with the option by keyword selected. Follow the link
to ball & lead screw assemblies that comes up.
1-1/4" dia aluminum or brass - aprox 6" length required
3/4" dia steel rod - aprox 3'
Special Tools required
Tap to thread ball nut to machine adapters
Die for X axis
Die for Y axis
Pictures of the X axis ballscrew and ball nut
If this project sounds a little too big for you consider the ballscrew
kit offered by C & G Research.
Click
to visit C & G Research